March 22, 2006
Saturday, we rolled on the Shovelhead restoration. The
crankshaft was pressed out of the case and we began the tedious task of masking
off the engine cases and transmission in preparation for paint.
Last Saturday I managed to mangle a finger and destroy
the high low beam switch. I needed to enlarge the mounting holes to allow them
to fit. If you remember the switches have had their wiring routed through the
handle bars, I drilled out the mounting holes while holding the switches in my
hand. Needless to say I got away with this three times until the last switch.
Then the drill cocked in the hole and grabbed the switch out of my hand and
beat the crap out of my finger. It also twisted the switch wires around the
drill bit and ripped them out of the switch. I figured the switch would have to
be replaced; I was more concerned about my bleeding fingers to investigate it
further.
Estle took the time to examine the switch and he fiddled
with it until he got it apart and asked me if we could just break the solder
connections and redo the wires and solder them back. We had an abundance of
wire sticking out and it looked pretty easy. After a few minutes we were
repairing the switch and it was reinstalled. He kidded with me, telling me that
we didn't budget for another switch, so I was lucky we were able to fix that
one.
We stopped work to make a short trip over to Casey Cycle
to get some PJ1 Fast Black engine paint, only to discover they close at 4. We
were just a few minutes too late. Without paint we came back and went on to
finish up some more of the wiring At that point we were pretty much finished
for this Saturday.
March 29, 2006
It's funny how a little thing can happen to make it look
like you really have made some progress. The Shovelhead's engine cases are
painted and I have reinstalled the crankshaft. This required a special tool, a
puller to draw the crank shaft into the bearing housed in the left side case.
Being the inventive sort, I drilled a hole in a steel plate and used the
compensating sprocket nut to draw the crank into the case. I stacked some
sockets under the plate and as I cranked down on the nut it pulled the shaft
into the bearing race. Sounds pretty easy now, but for a while there I was
stumped. I didn't have a drill bit big enough. After some time with my grinder
and a rotary file it was made to fit. Simple fix to a simple problem; I did
have to set it up twice, the nut ran out of travel but it worked.
All that's left is to seal the case halves and bolt the
case halves together. My excitement is growing because now I can get to the
part I really love to do, the engine rebuild. We have been waiting to get to
this point for several weeks, actually all winter. The transmission needs two
gaskets and it can be installed into the frame now that it's been painted too.
The rebuilding of the engine is one those milestones in
the project, and of course once it's in the frame the whole project seems to
take on a real life of its own. Something is just so right when you tear one
apart and then put it all together and it lights off for the first time. It
must be the same thrill Dr. Frankenstein had when he first zapped his creation
with electricity and he came to life
all of the work was worth that first
moment of life. Of course for us we don't need to worry about the towns folks
showing up with pitch forks and torches to kill the new creation.
We are planning a light off party the day we fire the
engine for the first time. So far I have not had one of my children not fire up
on first touch of the starter button. The Sporty project took more than a
couple of kicks to get it fired up but then I refused to kick it, and the owner
didn't have the starting procedure down. But I have to tell you it was me who
got it fired the first time. The old bald headed guy didn't forget how to kick
start a motorcycle. (It did however remind me why an electric start is better.)
After that it would fire up on the first kick if you did everything right.
April 2, 2006
Tuesday night after a quite dinner I went out to the
garage determined to get something done on the Shovelhead Project. I started to
apply the gasket maker to the right side crankcase. When I started to do the
left side I saw it needed to be cleaned a little better than it was. This also
required pressing the crankshaft out once again. After cleaning the contact
area and drawing the crankshaft back into the case; I spread the gasket maker
on the left case.
So far pretty simple; not that both case halves were
ready to come together I remembered the studs were still in the cleaning tank
being degreased. I quickly dried them off and wire brushed them and ran a die
over several of them to fix some mangled threads. Remember the gasket stuff is
now curing, thankfully very slowly. Now the studs are not all the same, some
are different lengths, and two are actually a different diameter. A quick look
at the service manual and each one is described and its location shown; I was
ready.
Now I picked up the left crankcase with the installed crankshaft
and carried it to the bench. I couldn't flip it over and insert it into the
right side case so I set it back down on the milk crate. I also took some time
to clean off the gasket goo from me and my clothes. I carried the right case
over and set it over the crankshaft and mated them up. Using the bigger studs
according to the service manual I pushed them in to align the case halves,
evening up the nuts (insuring an equal amount of threads on each end) and
finished installing the remaining studs.
Hey there are two holes still open? A quick look at the
service manual and there are two bolts that go in there too. After an
exhaustive and rampant search I couldn't find them or any to replace them. Now
I don't normally let mechanical things get the best of me but all I could think
of was not getting a good seal. There is no gasket between the case halves,
just the gasket goo.
In a rush I picked up the engine crankcase and set it on
the engine stand on the bench. Ok not being the strongest guy and the crank
shaft is pretty heavy by itself never mind in the cases. I picked it up and
with great care I held the whole thing close to my body. Well the gasket goo
was oozing out of the joint and all over me. Now I am angry. I set the engine
on the stand and began trying to get the goo off of me. My hands where covered
in it, my shirt was protected by my bib, yes I wear bibs to work and was still
in my work clothes, thank goodness.
Ok after getting as much of the goo off as I could I
commenced to tighten up the studs. Well being the worrier; am I getting a good
seal? I guess I may have used a tad more of the goo than was needed. But as I
worked the pattern of studs to tighten the cases together the stuff was oozing
out of the joint at a rather prodigious rate; in fact a lot of the stuff came
out, actually most of it came out. That's a good thing but I was collecting the
stuff with a rag, and it was getting all over everything, including me. Once
again I stopped to clean me up some and tighten up the studs. I'm sure I got
the best seal possible. At least the pockets on my bibs are now
waterproof
As you can see from the pictures, Saturday we pretty much
finished up the transmission and installed it in the frame. The next task is to
clean the benches good and start the re-assembling of the engine.
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