January 18, 2006
Saturday afternoon, after a trip to Hop's Place (they
specialize in automotive machine work and engine repair - one of the best in
the area) in wet downtown Hampton to drop off the Shovel's heads for repair; we
spent the rest of the afternoon ciphering out the wiring diagram for the old
Shovelhead. It was raining anyway and this task will sooner or later have to be
done. After unpacking the new retro wire harness, and diligently checking their
length and colors we routed about 60% of the bikes wiring. They're lots of tags
on the ends of the wires to indicate what they will eventually be attached to.
All of this electrical wire routing brought to mind the
some of the other things we will be looking for. Voltage regulators today are
all electronic, this old girl has a electrical mechanical regulator made by
Delco Remy, looks like it came off an old Chevy. That gave me an idea to check
the auto parts stores and see if we can't find one similar to it that will work
and save a couple of bucks. The starter relay is another item we are going to
have to search out too. Of course a new dash is on order also, we used the old
dash mounting plate for a guide.
Good news, after blowing out the dead bugs from the old
bikes horn and after hooking it up to a live battery it honked loud and long in
the garage. Estle said it never worked before but it does now. Miracles never
cease.
Being Monday was a holiday and I was off; Estle and I ran
all over getting some things taken care of. We called Hop's and got some good
news they will be able to repair the heads and it should be about a week or so
and we will get them back. We also went to Williamsburg to visit with Art at
Peninsular Custom Coaters and drop off some more parts for powder coating. Then
we ran over to Tidewater Motorcycle to get the tires mounted on the rims.
Back
February 2, 2006
Saturday we did a little painting; some of the small
parts to complete the triple trees and then when hunting for light bulbs and a
press. We went looking for a Hydraulic press at Northern, the only one they had
that would do the job we wanted was almost 400 bucks. Estle and I figured we
could build what we needed for a lot less. Now the light bulbs that was a
different matter; I had installed these nifty little turn signals (spelled
AFTERMARKET) on my CBR and they use a very non standard light bulb. I visited
several shops only to leave empty handed.
Estle and I stopped by Hampton Roads Harley Davidson in
the quest for light bulbs. Estle has been having a very hard time deciding what
color to paint the Shovelhead. It didn't get easier as he looked over all the
bikes on the showroom floor. I think we are looking at an electric metallic
blue, Harley Davidson calls it Cobalt. We left but not before finding out they
were out of stock in the special hard to find light bulbs.
A short ride up the road to Redline Motorsports, after a
minute or five of gazing at some fine Italian machinery (Ducati's on the
showroom floor) and the young man behind the counter materialized from the back
room with four of my hard to find light bulbs. Happily I paid for them and we
were off and headed to the house.
When we got back, the parts I painted before leaving were
dry enough to go back on the bike, we decided to remove a broken bolt from the
front fender mounts on the one of the fork sliders first. Removing broken bolts
is a tricky thing at best, steel bolts in aluminum seem to have their own
peculiarities. If your lucky the bolt will have broke off leaving a nice flat
surface to work with, but that is seldom the case. If it breaks off and leaves
some of it standing above the hole in most cases a pair of pliers will remove
the bolt if it hasn't been tighten down to the bottom of the hole or been there
so long it's become rust welded in place.
Our bolt was nice and flat, but about two threads below
the surface of the fender boss. With great skill and an excellent eye (and
bifocals) I center-punched the bolt, then with a very small drill below a 1/8
", we attempted to drill through the center of the bolts body. If the drill was
a tad sharper it might have worked, but it ran off to the side under pressure.
I went for another drill a little larger and sharper.
Now we were making a hole but unfortunately it was off
center. We attempted to use an easy out to remove the old bolt, but it refused
to move. Now we decided to drill hole out a bit larger trying to remove as much
of the bolt as possible; this required drilling in at an angle to move our hole
into the center of the bolt body. A 5/16 bolt doesn't leave you much room to
work in. Our next drill was 17/64" and it was sharp. It was one of the drills
sharpened on Estle's Drill Doctor. The screw gods were smiling down on us
because the hole went to the center and I must have been holding my mouth just
right as I straighten out the drill to go through right down the bolts center.
Chips and shavings were flying out of the hole at an
unbelievable rate when all of sudden smack pow; we were covered in plastic. My
thirty year old Craftsman drill exploded into plastic fragments when its
bearing went. I switched to an even older drill, one without the variable speed
or reversing modes, you know the same kind your grandfather or in my case my
dad owned.
We finished up the hole, inserted a tap and began to
clean out the debris. Tapping holes is an art I have mastered in the shipyard,
and by the time we finished up we had a very nice clean tapped hole which other
than some marks at the very bottom of the bolt hole, it looked factory fresh.
Sometimes it pays to be more lucky than skilled
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